| -On/Off Switch | -Main Distribution Panel |
| -Worklight | -Blade Welder |
| -Main Power Input Safety Switch | -Thermal Cutout |
| -Motor | -Blade Grinder |
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Here's the safety switch. This is where house power is wired into the saw. It's in excellent shape, other than the flammable dust pile sitting at the bottom. It was "union made" by the General Switch Corporation in Brooklyn, NY. It's not clear whether this box is original.Some things make it look like a later retrofit, some things make it look original. I've seen lots of pictures of other Doall bandsaws from the same era as this one; some have a different box at this location, some have no such box. More than likely, the box was a custom-install based upon code requirements in the specific location at which the saw was in operation. |
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| Here's the on/off switch (shown with the cover removed): |
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This was made by Cutler-Hammer, which is now owned by Eaton.
The
most amazing thing about the switch is the label I found inside the
box, in perfect condition. It indicates a build date of July 1940!
And it still
works! I can only imagine how many hundreds of thousands of cycles this thing has seen in 65 years. The switch on my 2003-built Delta Shopmaster drill press broke in less than 2 years, after maybe 500 cycles. This is a real piece of history. I find it interesting that even in 1940 they printed "Made in U.S.A." on things. I would have thought that unnecessary - wasn't everything made here in the US back then? I guess not. |
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| Here's the new electrical plans. Note that the wire
labels "U", "V", and "W" indicate physical labels applied to those
wires as they were installed for easier identification. The new arrangement represents a simplification of the original design and a slight increase in safety. Whereas the old design uses a 3-pole switch to turn the motor on and off, this new design uses 2 simple momentary pushbuttons to actuate a contactor. This is marginally safer, since full motor current is no longer carried to the switchblock, and in case of a power outage the saw cannot restart when power is restored. Note the safety switch has been eliminated, and the entire electrical system now fits within the main distribution housing, as DoAll originally intended. Also note the incorporation of an hourmeter, which will permit more accurate preventative maintenance. Main power is provided via 30 amp 10/4 SOOW service cord carrying two hot poles (red and black), one neutral line (white), and a ground. Power transfers to the main bus using an Amphenol MIL-spec circular connector rated to at least 46 amp. Internal main power distribution is carried by 8 ga. stranded THHN (rated to at least 70 amp). Secondary power (for the hourmeter and contactor coil) is carried by 16 ga. SXL stranded wire. The new motor provides its own internal thermal protection, so the reader will note the absence of any external protection. Power connection to the motor is via an Amphenol 97-3106A-20-4S plug and 97-3102A-20-4P box mount receptacle. This is rated to only 23 amp, although the wiring harness is rated to 70. The motor is internally wired using 16 ga. wire. I decided to reuse the original-equipment fuseblock rather than implementing a new circuit-breaker arrangement. There's no point in re-inventing the wheel when the fuses work fine and are conveniently sized to fit precisely within the main junction box. This system was tested 20 June 07 and functioned precisely as designed. |
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