Step 2: Remove Secondary Shaft Ball Bearing Here's the pressing operation to remove the secondary shaft ball bearing. That's a 5-ton puller, and the bearing was difficult to press off. It's a 6204 bearing, which is for a 20mm shaft. The secondary shaft measures 0.791" at the bearing mount, representing an interference of 0.004" with the 20mm 6204. According to Machinery's Handbook, the acceptable range of shaft diameters for this bearing is +0.011 to +0.002 for an interference fit. The condition of this bearing and the "modern" specifier "6204" stamped in the shield makes me think it's not original. |
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Step 3: Remove output shaft assembly The output shaft ball bearing is in pretty good shape, but has no numbers stamped in it. To make matters worse, the parts manual lists 4 separate Doall part numbers for the bearing, depending on the manufacturer (SKF, Norma-Hoffmann, NDWC, and Hoover). To complicate things even more, there are 4 different bearing covers, depending on which bearing manufacturer was used. The bearing on this unit happens to be an SKF. After searching online for interchanges for those numbers I came up empty-handed. I contacted Doall for help, but they never returned my call. This is the first problem encountered with the box. It will be very difficult to remove due to close clearances with the output shaft gear (can't get a puller in there to grab it). The bearing measures out with an OD of 62mm and a width of 19mm. Some time searching the NTN catalog indicated an NTN number 8506 single-side sealed bearing should be an exact match. I bought an 8506 and although it's dimensionally correct for this application, it doesn't have the same outer shield on it. That means it won't quite fit the bearing cover plate, but I think it would work fine nevertheless. In the end, I didn't replace the bearing because after cleaning this part up it seems to work just fine. |
| Step 5: Remove Input Shaft To remove the input shaft, the transmission is flipped over and the rear bearing cover is removed. This permits pressing out the input shaft. |
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| Step 1: press the input shaft (with input shaft ball bearing already installed) into the gearcase. | ![]() Setup to press |
![]() Press: 1-1/2" socket used to distribute load to the outer race only. |
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![]() Finished |
| Step 2: press in center bearing. This one's a little more complex because it uses a tight press fit on the input shaft and a light press fit in the dividing plate in the gearbox. As a result, it's important to support the input shaft during the press in order to prevent pressing the input shaft back out of the case (the input shaft ball bearing is also a tight press on the input shaft and light press in the case). I cut a block of wood to serve as support for the input shaft as shown. | ![]() Block installed to support input shaft during press |
![]() Inside of gearbox with center bearing removed to show nice clean gears |
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![]() Center bearing in place before pressing |
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![]() Finished. Note the same 1-1/2" socket was used during this pressing operation as in the previous press to apply load only to the outer race. |
| Step
4: install
secondary shaft ball bearing.
Had a little trouble with this one. As I commented
in the
disassembly, this bearing was a very tight interference fit.
It
made the pressing operation almost impossible - I couldn't get the
bearing to press on straight.
I ended up taking a smooth mill file to the secondary shaft
and
removing a thousandth or so, which made the pressing operation a piece
of cake. In fact, it was so easy (maybe 500-700 lb) there was
no
need to support the opposite end of the secondary shaft to prevent it
from moving axially during the press. This is convenient
because
supporting that shaft on my arbor press would've been a real challenge. At this point most of the mechanicals for the gearbox are finished. Next up is gaskets. I bought a sheet of Buna-N (1/16") to cut gaskets for the front and rear bearing covers and the case flange. This stuff is easy to cut and relatively cheap. |
![]() Press. No need for a socket to distribute load. |
![]() Finished
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I also built a simple test stand for the gearbox. My plan was
to
eventually fill the box with oil and run it for a little while using my
1/2" drill. This required the test stand and a shaft adaptor
(because the input shaft is 3/4" diameter, so it won't fit in a 1/2"
drill chuck). This picture shows the test stand (made from scrap lumber) and the gearbox with shaft adaptor attached. The shaft adaptor is a piece of 1" square aluminum bored 3/4" on one side and 1/2" on the other. A 1/4-20 bolt acts as a set screw to retain a piece of 1/2" dowel rod that the drill chuck holds. This works, but the holes in the adaptor aren't quite concentric with the gearbox input shaft (owing in large part to my primitive tooling). I have since filled the gearbox and it's been sitting there full of oil for several months without even the slightest leakage. I've also spun up the input shaft with an electric drill to get everything coated with oil. Everything works perfectly. |
| Problem 1: secondary shaft bearing Two important problems were encountered when trying to reattach the bearing covers. Both involve the secondary shaft. As I commented earlier, I had to press the secondary shaft toward the input side of the transmission to relieve a binding that was occuring as the big first gear on the secondary shaft contacted the center bearing during roughly 1/2 its rotation. In so doing, I pushed the secondary shaft ball bearing out of the case by 10 or 20 thousandths. This is a problem because it prevents the steel cover from fitting flush with the surface of the case. To fix this, I have to make a riser plate out of 1/8" aluminum. The riser will move the cover plate up away from the bearing and permit a good gasket seal. A picture of the riser plate is below. I cut it out with a jig saw (ironically, a bandsaw would've really come in handy for this). I adhered it to the gear case using silicone gasket maker. |
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| Problem 2: axial movement of output shaft The second problem lies at the opposite end of the transmission. The output shaft bearing is not press-fit into the case. As a result, once the unit is assembled the output shaft is free to move axially. Normally this wouldn't be a problem, except that when the shaft is fully extended away from the case the output shaft gear makes contact with the secondary shaft ball bearing, causing a bind. I'm not talking about a lot of movement - maybe 0.050" or so. To fix this problem, I cut a 1/32" piece of PTFE sheet gasket into an annulus properly dimensioned to occupy the space between the cover plate and the output shaft bearing. With the cover plate in place, then, the PTFE ring makes contact with the steel plate and prevents any axial movement of the output shaft. Notice that axial loading from the helical gearset will tend to pull the output shaft inward, toward the back side of the transmission (which is good). There is a potential problem with this solution. The output shaft must transmit the blade tension to the output shaft bearing, then into the case. If the blade tension causes an axial component of force pulling the output shaft out of the transmission, all that axial load will be handled by the bearing cover plate (next picture). That bearing cover plate isn't strong enough to take much load. I hope, therefore, that axial loading due to band tension is very small. |
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This works remarkably well. Here's what it looks like with
the cover plate and new gasket installed. You can't actually see the PTFE ring with the cover in place. I spent some time straightening up that front cover - it was mangled pretty badly. |
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Before |
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After. In this photo the shift lever locking ring is installed backwards. I fixed it after this picture was taken. |
| Application | Gates Number | Standard Size | Length (in) | Circumference (in) | Max. Width (in) | Height (in) |
| Motor to air pump | 2260 | 4L260 | 1/2 | 5/16 | ||
| Motor to VSD | 3370 | 5L370 | 36.92 | 37 | 21/32 | 3/8 |
| VSD to gearbox | 3510 | 5L510 | 50.94 | 51 | 21/32 | 3/8 |
| Gearbox to speed indicator | 1290 | 3L290 | 28.68 | 29 | 3/8 | 7/32 |
| Application | Gates Number | Standard Size | Length (in) | Circumference (in) | Max. Width (in) | Height (in) |
| Motor to VSD | 3340 | 5L540 | 53.94 | 54 | 21/32 | 3/8 |
| VSD to gearbox | 3540 | 5L340 | 33.91 | 34 | 21/32 | 3/8 |