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The speed indicator was
non-functional. It's belt was missing, and when the driver
was spun manually the entire mechanism made an awful racket and
the needle wouldn't move. This gauge functions
exactly like any ordinary mechanical speedometer, which means it uses a
flexible drive cable, so I assumed that cable was broken. Notice the glass is also broken. It's mounted in the saw shell (just above the blade welder) using four bolts as shown. The bezel (painted red) is simply pressed into the gauge case and is pried out using a screwdriver (gently, so as not to bend it). Once the bolts and bezel are removed, the entire assembly can be removed from the shell. |
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On the one hand, it's good that the cable isn't broken. On
the
other hand, that means the problem is in the gauge itself.
Having
never repaired an instrument like this before, it took some time to
figure out how it works. Here's a couple pictures of the
gauge
internals, partially dismantled. The first is a face-on shot
looking at the front of the gauge mechanism with the face removed (not
the clearest picture ever, but the best my camera can manage). I could spend several boring paragraphs attempting to describe how this works, but even with pictures it would be virtually incomprehensible to anyone who hasn't dismantled one before. The basic principle is a rotating magnet on the input shaft which spins inside a steel "drum" to which is connected the gauge needle shaft and a tiny clockspring. The delicate interaction of that rotating magnet with the drum, needle shaft, and clockspring causes the needle movement around the gauge. An ingenious mechanism, but extremely fragile. Remarkably, I think I managed to repair this thing. Of course, during the repair I completely uncalibrated it. But it now indicates a speed when I spin the input shaft with an electric drill, so after the saw is back in working order I can recalibrate it (there's actually a simple adjustment mechanism within the gauge that acts on that tiny clockspring I mentioned earlier). |
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Next is the gauge driver, which is really just a simple bearing with a
pulley on the end to transfer rotation to the flexible cable. Although it appears the shaft can be removed from the bearing, it can't. Of course, that didn't stop me from trying to remove it by force (5 ton puller, lots of hammering). Unfortunately, the bearing must be replaced as a complete unit and I can't see any way to properly service it. It needs service - it's binding through 1/2 its rotation. The good news is this is an exceptionally simple part, and I could probably make myself a replacement using a couple standard bearings. I soaked it in parts solvent for a few days in the hopes of loosening accumulated oil sludge. Then I soaked it in SAE 5w-20 detergent motor oil for several months. |
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| Before | After |
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